Saturday, 28 January 2023

Boring out the spindle nose adaptor body

I made a start on this some months ago on the Bantam but it struggled to overcome the cutting load. This was with the motor in high range ie ~1:1 ratio, yet I needed something like 500rpm. The right solution would have been to change the gear ratio, along with the corresponding settings in LinuxCNC but TBH I couldn't be arsed - and I thought I had a chuck for the Tree when I acquired that dodgy Kitagawa chuck. Now I have a better solution that will allow me to learn about the Tree.

Let's get it mounted in the newly fitted 4-jaw:


It's fairly concentric - or at least good enough, given that I am about to do some roughing out:



New pulley for the motor:
But first, I need to fit a smaller pulley on the motor. Currently I have a 300mm pulley on the motor and 160mm on the motor. That would give the best part of 6000rpm, which would be fine for a small collet chuck but way over the top for a 6" chuck with a max speed rating of 2000rpm. Instead, I'll fit a 118mm pulley on the motor, giving a 3:4 reduction. With a 3000rpm motor, this would theoretically deliver a top speed of 2250rpm, which is better. And when I am down around the 500-1000rpm range, the 4kW motor might stand a chance of cutting some decent chips.


Here's the current setup:


I also have a small pulley behind, although perhaps that was a bit on the small side. I simply chose the smallest that was available for a 28mm shaft.



That's better. The 300mm pulley is still on the motor, but this time it's at the back. The shorter belt worked out well. I calculated the required length quite simply from the difference between the pitch diameters (multiplied by 0.5 x Pi). Good. Now we are finally ready for action.


Let's make some chips then!
The new 20mm boring bar is rather longer than I need, so I will chop it down a bit. Besides, I bought 2 with that in mind. I need about 80mm stickout on this job, so I'll chop off about 50mm.


It's not hardened, so the bandsaw copes fine:


Ready for action:


Off we go:


Quick skim passes in X and Z, then measure it up so I can tell the machine where the tool tip is.


Let's do it:


No video, it didn't happen:


One consequence of taking girlie cuts is that the final finishing pass resulted in some squealing and a slightly patterned finish. If I'm going to do this with indexable tools, I should use a ground / honed insert I suppose. But it's not a functional surface, so I can live with it for now.


A final observation - running the machine with the hydraulic pump off results in a shitty surface finish and hellish chatter. I think we can conclude that although there may be some residual pressure on the turret, it's not enough to ensure rigidity of the tool. That probably shouldn't be a surprise but I was wondering and now I know.

No comments:

Post a Comment

TIG welder up and running - after some fault diagnostics and repair

Finally got some time to connect up the flow meter and argon hose. Plugged in the torch and ground cables and the torch hose etc. Powered it...